1997 Maxima Code P0340, No Start or Start and Stall

This 1997 Nissan Maxima was towed in from another shop after unsuccessful repair attempts. I am not sure how many shops it has been to. Tried to crank vehicle, it spit and coughed and jumped and carried on but I managed to get it to fire a little by depessing the gas pedal to the floor {clear flood mode}.

I checked the plugs and they were black and fouled out and several showed signs of gas blowby at the insulator seal, so I installed a new set of plugs. cranked the engine and it ran. After a couple of minutes it had cleared up and was running good. Ran a few more minutes for good measure. Turned engine off and recranked. It cranked and ran fine. Did the other shops miss something this simple? I don’t know? Cranked it several times and no problems, time for a test drive. Backed the car out of the shop and took off on a test drive. Right, got 20 feet and it stalled and would not crank back up. Kind of figured it, plugs would be too easy.

Got the scanner out and checked codes P0325 and P0340 were stored. The P0325 code is for a knock sensor and will not cause the engine to not run, so I was going to concentrate on the P0340 code. The code P0340 is for a cam sensor error. Checked the cam sensor and it had been replaced.

I needed to check the continuity of the wires between the cam sensor and the ECM. The ECM is located under the center of the dash as shown below.

I removed the white plastic cover to have better access to the wiring.

I had to use an ohm meter hooked to both ends of the two wires. While the harness (shown below) was wiggled. Sure enough one of the two wires was broken. In doing this repair I had to try several things before I came up with a way to repair this vehicle in a cost effective way. The harness costs about two thousand dollars plus installation.

I clipped the two wires near the ECM harness connector. Then started to look for a way to run new wires.  My first choice would be to attach new wires to the old, with splicing connectors and pull them through the harness, then splice at the other end.  This would not work as the wires are glued into the grommet at the firewall. It would be virtually impossible for me to identify the two wires at the ECM so you will need to access that information from Mitchell 1. There is a link at the top right of this page.

My next choice was to try and run the new wires through, hopefully another grommet. The problem is the only other thing I could see was the a/c drain tube. Running new wires there did not seem like a good idea. To get a really good look the evaporator case needed to come out. Recovered the refrigerant and removed all of the interior mounting screws.

Problem, the evaporator case will not come out past the glove box support brace. A very close look and I determined that if I removed the metal brace. Then cut the plastic between the two screw holes on each side that the evaporator case would come out. When reassembling the two screws would hold the plastic pieces together. It appears to me that an engineer actually designed it to be cut, if the evaporator case needed to be removed.

The cut on the right side of the glove box opening.

At least now I can see where the wires go through the firewall. I felt around and decided that I could go through the original grommet. On the lower right side, as it is viewed in the pictures below.

I have a special tool for doing this procedure. The tool is similar to a screwdriver but it has hole running through it. Using the sharp end I pierced the grommet and ran the wire through the hole in the tool.

With the wire run through the hole in the tool and to the other side of the firewall, I pulled the tool back out over the remaining wire on the inside of the vehicle.

A close up look at the hole in the handle.

The sharp end of the tool that easily pierces the rubber grommet.

I purchased a special piece of shielded, twisted, pair wire cable from an aircraft supplier. The first thing that had to be done was to loosen  the shielding and move it down the cable assembly enough to stagger the joints. I did have to split it length way also.

After prepping the cable, I connected it to the factory harness connector. I staggered the joints.

Heated the tubing and shrank it into place.

Twisted the remaining cable, around the repair.

Pulled the shielding back up and around the spliced wires, then used tape to hold it in place.

I repeated the process at the other end near the computer. I then taped and wire tied the new cable to the old harness. One thing that I learned through this whole experience is that if at all possible do not pull the harness out from under the dash. It is looped to the top of the ECM and is almost impossible to get it back into place. The reason I had pulled it out was so that I could pull the new wiring through the old harness and just attach it on both ends. The glue in the fire wall grommet prevented me from doing this, so in the end, there was no reason to pull the harness loose that far.

A closer look at where the wiring breaks inside the harness.  My experience on this one also convinced me to not open the harness to actually see the damage. Way too hard to get it all back together that way. Just make sure the wiring is the problem with a meter and/or piggy back  a new harness to the outside of the old harness and attach it at both ends.

1999 Ford F150, P0306 Misfire Cylinder #6

This 1999 Ford F150 Came in with a misfire on cylinder number 6. No big deal except that the spark plugs, spark plug wires and coil assembly have already been changed with quality parts. The other thing I noticed was that the misfire did not come in until the engine speed reached about 1500 RPMs. Diagnosing this wound up being easy after I thought about it for a little while.

To confirm the cause, note the RPM range when the misfire comes in. Disconnect the EGR valve vacuum hose and plug the hose end. Bring the RPMs back into the misfire range as previously noted. If the misfire is gone the EGR tubes are restricted.

To correct the condition, remove the upper intake and inspect the EGR orifices in the lower intake openings. I did not bother listing how to remove the upper intake, as that information is available in any repair manual for this vehicle.

The picture may be too dark but there are tubes with holes in them where I am pointing to.

A small piece of wire and a good shop vacuum and the debris (at least in my case) comes out easily. The same condition could have caused a misfire on any of the cylinders. Just coincidence that the #6 tube was open and the others were highly restricted. The one open tube was causing all of the exhaust air from the opened EGR valve to be dumped into cylinder #6. Thus causing a lean misfire on that cylinder.

Some new gaskets, put it back together and this one is done.

2003 Chevrolet Impala, Battery Goes Dead

This 2003 Chevrolet Impala came in with the complaint that the battery would go dead after a couple of days of driving. The customer stated that the battery light had been coming on and going off for a while now. The alternator has been replaced three times and the battery twice. The battery light was on, so I checked the basic charging system first. Hooked up my tester.

Cranked the engine and checked the meter. Not charging.

I decided to check the alternator output at the back of the alternator.

Well, twenty plus volts is pretty high. I have seen this problem multiple times on many different vehicles. The cause is an open circuit between the alternator and the battery.

This was the voltage with the engine off. A slight amount of voltage was present, so I was thinking a loose connection. Rather than a completely open circuit caused by a blown fuse or fusible link.

Looking over the engine compartment, I saw that the alternator output lead headed back to the starter. Pretty obvious that there is a problem there. Click on the picture below to enlarge for a better view.

I removed the nut and lock washer so that I could clean the mess up and check for deeper damage.

The ring terminals were arced up but they cleaned up well.

After thoroughly cleaning the ring terminals I found only cosmetic damage. I reassembled the wiring to that battery post on the starter. Installed a new nut and washer.

Check for voltage at the alternator with the engine off.

With the engine on.

I rechecked at the battery with my  big tester and all was well, except that the battery was down, as indicated by slightly high amp reading and slightly low voltage reading.

A little time on the battery charger and this one will be ready to go.

2004 Ford Expedition, P0305 Misfire Cylinder #5

This 2004 Ford Expedition came in with a code P0305, misfire cylinder #5. The customer already had the spark plugs changed out a few days ago, but his misfire was back. Time to get to cylinder #5 coil. I removed the two bolts that held the engine cover in place.

After the top engine cover was removed, I could now get to the power steering bracket that covers the #5 coil assembly.

There are three bolts that hold the bracket on place. All 8 mm heads.

Now, unplug the coil and only one 7 mm headed bolt holds the coil in place.

Pull the coil out and inspect.

There is the misfire, right on the side of the coil. A new coil assembly and all is well.

This coil should have never been reinstalled when the spark plugs were changed. As a rule of thumb for myself, if there is a specific misfire on one cylinder, that coil is going to be replaced, when the tune up work is done. At the very least it will be moved to the easiest location for removal. This one was pretty easy but never put a suspect coil back in #3, #4, #7 or #8.